Work Session

May 16, 2020

 

To join the fun, contact the railroad at: WorkSession @ RedRiverAndGulf.net (no spaces)

 

Team:
Michael Miller, Tucker Baker, Gerald Winegeart
 

On Friday I was at the museum and first inspected switches #9 and #10 (in regards to a minor derailment earlier in the week), the switches to the engine house tracks. Gerald was mowing nearby and wanted to see how the switches were as well. He watched as I went over both switches multiple times with M2 (A4 motor car) and both switches appeared in good order and the car ran smoothly over both. I did rake out and remove a great deal of leaves and pine straw from both switch points before hand (photo attached). While ties are needed in the area, both switch points are in good order, in good condition, gauged decently, and operate smoothly when closed and locked properly. Switch #10, to the second engine house track where the M4 railbus normally resides over the pit, does have a switch stand that moves when the switch is thrown, but closes and locks securely when the bar is properly int he down position. The whole area of track is formally on my radar for improved maintenance.

While I had the M2 out of the engine house, I gave her a good sweep out and cleaned all windows (photos attached). You have problem, fix it with Windex! The wasps were not pleased to loose their home, but I certainly removed them promptly...

Speaking of varmints, I did take a gander at Mike and team's great work on 106 and found a benign king snake sitting next to the log car coupler to the tender. I will admit, his rodent work is needed but shoot dang it gave me quite a jump!

I didn't have nor could find a key to the M4 railbus to run her over the switches as test and to clean her out outside of the engine house. I'll try to get that down next weekend when I'm back at Longleaf.

I did a quick inventory of rail material available on hand and discussed with Mike. We agreed that the existing rail in the machine shop track can be reused and will be sufficient with good material underneath solid and fresh ties. We have enough ties on hand and new nuts, bolts, and washers for this track relay work. Friday afternoon, using Rust Buster spray and track wrenches, took apart half of the nuts and bolts on the track joint bars.

Saturday, Mike used a smokeless wrench (cutting torch) to remove the remaining nuts/bolts on the track bolts I could not budge. Using the tractor and chains, we removed and placed inside the machine shop 4 rails (2 panels in length) and their joint bars. We then used the tractor to remove the loose sand material. Mike is working on sourcing a small amount of pit run gravel to use as base fill material underneath this track we'll rebuilt. We have about 2/3 of the old fill material removed via tractor. We placed the taken out dirt behind the engine house near the camping area, but out of the way and right behind the damaged storage shed. It can be used for other projects as needed. The machine shop rail is light, about 45 pound rail or 50 at the most. We figured 2-3 inches fill material height, 8-9 inches for tie height, and 4 inches for the rail, so we dug down 16 inches. We will taper off to either end , so primary area to bring in new fill material will be where 202 will rest once returned back to place.

Saturday afternoon, tractor had 1/4 tank diesel and finishing mowing blade was still on, so we could get the tractor in to remove the remaining dirt we wanted to take out. I will be returning next weekend, so Mike and I will finish the remaining dirt work. It should take less than a full day to get the site dirt work prepped to how we'd like it.

Other notes:
Only 3 ties were underneath two panels of track we removed. Where 202 used to sit, these three ties more than likely prevented a 202 catastrophic rollover.

Upon removing dirt, we noticed that apparently the machine shop track we see had been re-laid over an existing grade, as multiple old ties about 4-6 inches underneath the dirt were found and no where near close to being gauge-holding ties. Many are cracked and can't be reused, but solid enough and Mike and I decided they would make excellent erosion controls placed adjacent to the wall pillars to keep machine shop dirt floor in. Will be incorporated into the track relay work.

The water drainage in the shop is under control, but a small amount still comes under the coal pile. To funnel out this trickle, Mike had a great idea to insert a small pipe between track ties on the new track to do directly out the shop. Upon inspecting the plastic nursery pipes in the engine house tender, these are irrigation pipes filled with small holes to let out water. Not good enough. Mike is searching for a good pipe or basin to use. It would be another good drainage improvement to the track relay.

-Tucker Baker
  RR&G Road Master